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Alternator Bracket
Text and photos by Bob Klowak

This is the beginning of more aluminum creations. You guessed right - 6061 quality, the good stuff. I get a bit carried away sometimes. Well we started out with a piece of ½" plywood and cut out what we thought would fit. It was a bit of measuring and scribing to get it to fit . I find cutting template from plywood is easy and quick and saves doing things twice.

Once the first bracket that mounted to the head was fitting properly, the last other one was close to match. The spreader pieces were fairly straight forward.

The three plywood templates were bolted to the head and the alternator was put in place and the belt was fitted. Everything seemed to be alrigh . Belt clearance was good and alignment seemed to be close.

At this point, the wood templates were removed then scribed on to the ½" plate of 6061 aluminum.

The pieces were then cut out and sanded together to match. The holes were marked but careful measurements were made to ensure a good match to the head bolts. Drilling the holes slightly larger made up for any errors in measurement.

After the pieces were tried for fitting and all went well, holes were scribed and drilled with a hole saw. Keep in mind to keep the drill speed to an absolute slow speed and put a lubricant on the cutters. After cutting out the holes a jig saw was used to complete the cut and sanding drums were used in the drill press to sand the interior.
After the sanding was done the brackets were assembled and fit very well except for one thing, the belt was very close to the front bracket . It was ¼" away and at high rpm's I felt the belt may wander and get cut up so I removed the rear bracket and extended it down in order to mount a belt tensioner.
As you can see a belt tensioner from a newer Ford truck seemed to just fit perfectly without any modifications. I did a torque check on most tensioners and found them to be at 30lbs. This also kept the belt in alignment and hopefully keep it from wandering.
After reinstalling the mount, I found the rear bracket was pressing against the rocker covers, so some thick washers were put between the plate and head(only one per hole was needed). This gave the clearance needed and also moved the whole assembly forward. Careful measurements to a reference point on the crank pulley and then the alternator pulley found they were dead on. We are now going to whip up the AC brackets so we can complete the pulley system.
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